By this time it is late September, and it dawned on me that I would be away on holiday when the MoT ran out in early November. Not a problem, as last year the car flew through! So I booked the next Monday afternoon off work to take the car in, giving me the weekend to prepare it. A good going over a week before with help of a friend indicated that there was nothing obviously wrong other than the handbrake being a little looser than it could be, so after a quick adjustment I was feeling confident. The next day the horn brush fell apart, but that's okay, I ordered another.
Fast forward next Sunday - the day before the MoT - I was driving to the supermarket and oh no! Massive plumes of smoke started pouring out from the steering column! No idea why it suddenly decided to go, but the indicator arm decided it had enough and fell apart and burst into flames. Not to worry, as I have a spare.. but on fitting it that spare doesn't like to go left unless you hold it in place. The new switch then decided follow the first and the wires snapped off the back. AARRGGHHHH.
Both switches were then cut open and I managed to build one good one out of two broken ones. The original casing (dated 11/70) was kept, the insides of the second switch were soldered to the wiring loom from the original and all put back together with a nut and bolt scavenged from an old wall socket (a perfect size!).
The inside of both switches were covered in a very thick coating of dried on grease and crud. With all this cleaned off and lightly lubricated, the switch now works a treat, and actually has a really nice feel to it - a big improvement on the soggy switch that was on the car before. Please excuse the poor photos, as I was in a hurry to get it refitted!!
I finally got everything back up and running again at 1am Monday morning.. phew!
Early the next morning, feeling confident I drove to the MoT station and left the car there before getting the tube to work. On the way I did hear a strange clonk after going over a speedbump, but couldn't see anything wrong and the car seemed fine..
At lunch I got the news.. FAIL. Booooooooo...
Went back to the garage, he said there were two things:
1. The front seat was insecure as one of the nuts had fallen off the base.. but he had already put a new nut on for me. Great!
2. The front o/s anti-roll bar mounting had rusted away and the mounting plate had disappeared up into the chassis..
The tester pointed it out to me, and yes, there was a giant hole directly underneath the roll bar mounting plate! It wasn't noticeable during my inspection, but it appears the plate had rusted from behind the roll bar mounting plate and the speedbump that morning had been the last straw. The MoT station didn't do welding repairs, but pointed me to a great little garage I'd never come across before. It was a proper little gem, hidden away in old railway arch and had been run by an older chap for decades - literally a couple of streets away from me. He told me to bring the car to him on Wednesday and he'd sort it.
He did a very neat job of the repair, and while it was a repair that is visible, the rot was totally cut out, the inside of the chassis painted, a new patch made out of thick steel folded over the clean metal and seam welded on. The roll bar mounting plate was cleaned up and welded back on over the top of the patch. A repair rather than a restoration, but very neatly done and very strong.
A quick trip back to the MoT station and a fresh ticket finally in my hands, the next hour was spent nattering about old cars
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1978 Triumph Dolomite Sprint (
project thread)
1966 Volkswagen 1300 (
project thread)
1962 Austin Mini (project)
1962 MGA 1600 Mark II
1965 Mobylette SP50 (project)
2001 Rover 75 2.5-litre V6